Replies: 1 comment 3 replies
-
Hi, I believe this was fixed in the latest version (v2.8.0) of ROSCO. |
Beta Was this translation helpful? Give feedback.
3 replies
Sign up for free
to join this conversation on GitHub.
Already have an account?
Sign in to comment
-
Hi,
I am using the ROSCO controller v2.7 with a 15Mw floating wind turbine.
When I have
Fl_Mode =2
, I see a big jump in the beginning of the simulation, as shown in the figure bellow. My floater and turbine initial conditions are set properly. What is the cause of this jump?In some cases the rotor speed goes to negative and fails to recover back. Do I need to change something in my DISCON.IN file to avoid this?
Best regards,
Beta Was this translation helpful? Give feedback.
All reactions